I am not sure when the Whitton truss bridge across the
Murrumbidgee River at Wagga had its overhead arch girders replaced with steel
beams, but it was before 1970. And I do
not know the reason, as the double track Whitton arch bridge at Albury over the
Murray River still has its arches
Shortly after being built in 1879, this NSW Archives picture shows the Wagga Wagga bridge, and the timber trestle |
In any case, I needed to model the Murrumbidgee bridge as it
appeared in 1970, and that meant scratch building the overhead “U” support
beams. The first part of the Murrumbidgee bridge blog
post is way back on the 26th June, 2017. I finished that blog post saying that I was
waiting for ABS styrene from China, or a source of brass “C” channel or the
correct size.
The bridge as it appeared in my June 2017 blog. |
To cut a long story short, the styrene “C” channels from
China were substandard, and I was unable to locate the correctly sized brass
“C” channel. However, I don’t like to
leave projects sitting around for too long, and I wanted a distraction from the
pain of shingles (yeah, that is another story), so a start was made.
The styrene “C” channels, whilst poor, could be
modified. I cut out 7.5 cm sections
that were more or less straight from the 50cm lengths supplied; and reduced the height down to approx
1.5mm. These I put into a jig to hold
them at the correct distance apart, whist I glued the styrene spacer plates
on. Unfortunately, removal of the jig
stressed the joints out, and the whole lot disintegrated. Better to find that out now, than after I had
spent any more time on them.
The failed girder attempt with styrene |
As no suitable brass “C’ channels were available. I had
little choice than to fabricate my own from strip brass. In this case I was very lucky. I had in my supply of North Yard brass strip,
enough 1.5 x 0.25 x 150mm, and 3.0 x 0.25 x 150mm strip pieces to fabricate the 3.15 metres of the “C” channels of the correct size for the bridge. Yes, that is a lot of brass strip
Parts needed to make one 150mm strip. This completed strip will be cut into two 7.5cm sections. This is a fortunate measurement, as it eliminates waste of the brass. |
Once the “C Channels” were made, I fitted them into the
distinctive “U” shape of the prototype, and matched a pair back to back, and
soldered spacers to hold them a scale foot apart.
Three 7.5cm sections make one half of the "U" beam |
One completed "U" beam. The spacer plates are 3mm strip brass. |
All these measurements have been guesstimated
from the prototype photos I took during the bridge replacement over a decade
ago
After being gas axed, the bridge truss sections were craned to one side awaiting removal. This view shows the interior construction of the girder quite well. |
To match the prototype, I will have to fabricate 7 “U” beam
supports, 4 on the first girder, and 3 on the second.
“U” beams were
secured to the bridge using triangle gusset shapes. These were made from sheet brass, but
soldered to the bridge with 144 degree C solder, rather than the 60/40 solder I
had used earlier. I did this for 2
reasons – a) I did not want to desolder
the assembled “U” girder upright, and b) 144 degrree solder can flow with my small 25 watt iron on the
large heatsink of brass that is the Whitton truss bridge side
One span, with two "U" beams fitted, and braced, and after removal of the temporary brace |
The result was very strong, and I felt confident to remove
the temporary brace, designed to stop the 2 bridge sides from collapsing
inwards with handling.
I made a minor change to the assembly order of the
subsequent “U” girders. Basically, the 2
uprights were installed, soldered, and braced, before the overhead beam
installed. This was a lot simpler than
my earlier method.
Detail soldering of one of the venter uprights |
Angle braces were fabricated, and soldered to all 4 “U” beam
assemblies. These are purely cosmetic on
my model.
I have been using fluxes to aid the soldering, and these need to be removed. I have scrubbed the girder with kitchen cream
cleanser, and washed the lot in water.
Further treatment will be needed prior to painting, but at least the
model is no longer a clothing stain hazard.
As you can see, I still have to fit "U" girder supports to the second
span. Followed by painting, and then the
sleepers and track can be added.
This process is very time consuming. I
have not added up the hours I have spent – but my last “U” beam assembly took
just over 5 hours to fabricate, and add. I am sure
that talented modellers might have used 3D printing to make the “U” beams - I am not in that category
Happy to report that after 3 weeks, the shingles pain has much
reduced. Whoever said Model Railways is
therapeutic must have had me in mind. I
will continue with fitting the “U” beams, and with luck, will have painted the
bridge for my next bridge blog post.
Happy modelling
Nice work Rob, still gathering items for my next bridge. I feel they can be frustrating.
ReplyDeleteBob
Well done Rob, I'm sure this bridge will become the scenic stand-out on your layout. Hope the New Year brings a break from any pain for you. At least our model trains are a welcome distraction to help us stay positive.
ReplyDeleteI have found the date when the overhead beams were replaced. 1928. The reason for this might be the anticipated introduction of the 57 class, where the loading gauge was affected. History shows that the 57 never ventured south of Junee, but that didn't stop the modifications to the infrastructure
ReplyDelete