I am pleased to report, that I have finally purchased a new slide to digital scanner. After some advice, I purchased a Plustek 8100 from TEDs camera store website on April 13th, and after 7 weeks, it arrived last week.
It took me a further 2 hrs to install the software, rapidly read through the manual, and then came the big test – results on the below picture.
|LVR 5367 taking water in October 1997. The original watering facilities at Wagga were out of use by this date, hence the local fire brigade did the honours|
|Ready to depart|
Of course, I will need to do more experimentation. It is nowhere near as fast as my cheap and cheerful scanner, but if the first scans with the Plustek 8100 are anything to go by, the quality exceeds my earlier Epson scanner, purchased in 2004, and still attached to the 2004 Dell desktop running Windows XP.
|The plustek scanner|
Enough of computers. Back to some modelling.
Brass loco repairs
Last weekend, a number of model train exhibitions, and the NMRA convention had been cancelled due to the COVID19 situation. So, instead of spending the whole weekend up in Sydney, I thought I would use the time to restore a few brass engines I had in a sorry state.
An ebay purchase, at a discount as the seller said it had some issues. First of all, it didn’t run. And second, was that the body did not sit correctly on the chassis.
Brass steam engines are generally easy to take apart, and the Bergs 30T is no exception.
|The inside of the Bergs 30T. The openframe motor uses plunger carbon brushes, and the insulation on the back of the frame is visible|
The first thing that I noticed was that there was a lot of insulation for the drawbar pivot wire going to the motor. This was interfering with the body mounting, and so the second problem was an easy one. The motor not running fault, is normally caused by a broken wire, but this was not the case. I unscrewed the motor, and disconnected the Delrin driveshaft coupling. Applying power directly to the motor terminals did not fix it. I was contemplating a can motor upgrade, but I thought I would check the carbon brushes (plungers). Well, one was worn down past the point of useful. I fitted a replacement, and success. Re-assembled, it looks, and runs OK. Sure, the motor is on borrowed time, and a can motor upgrade, along with DCC is in its future
|Bergs 30T model was made by Kumata (japan) around 1980.|
The loco would look better with a bogie tender, and this is where acquisition 2 comes in.
I swapped a surplus new DJH C32 kit for this one, sight unseen from a mate, who said apart from the lack of box, it was a good model. My thinking was that an assembled model would be a quick way to get a tender, and the Bergs C30T tender could be matched with the C32, and sold on. There were a number of C32s with 6 wheel tenders stabled at Broadmeadow in the 1950s, to allow them to turn on Maitland’s 50 foot turntable. Well, that was my thinking.
Unfortunately, my assessment of the C32 was nowhere as positive as my mate’s. But a deal is a deal, and brass models generally can be fixed
The model actually ran sweetly, which was nice. But the tender buffer beam had a warp, caused by someone’s earlier attempt to resolder a buffer that must have come loose. The ladder also was misshapen, although it was rebent back with pliers. The loco though had more issues. The missing cabside step, the unsoldered clack valve pipes, and the broken & missing brake hangers were cosmetic, although the front bufferbeam butchery to accommodate a #5 kadee coupler was ugly.
|The buchery on the front buffer beam to accomodate the Kadee coupler was nasty|
|Tender rear showing a minor buckle in the LHS buffer beam|
To repair the brass bodywork, the loco was disassembled. This is when I found another fault. The chassis frame spacer soldering had split apart in one area – which explains in part, why there was a plastic block glued to the underside of the body – “to stop the frame from flexing”. Struth.
|The frame sitting on the "plastic block" which was glued to the underside of the body. It looks soldered in this view, but that is an illusion. The split in the spacer for the chassis frame is also just visible|
Anyway, to cut a long story short, a new section of brass plate was whittled down to fit the bufferbeam “hole” and soldered in place. The plastic block removed, the chassis frame resoldered, and a rear cab step made from scratch and soldered.
|I cleaned up the hole as much as possible. And cleaned off the gold paint, back to raw, untarnished brass|
|From underside, the scratching of the brass was more ugly. The gold paint is extremely heavy|
|A new section of brass fitted, soldered, and cleaned up. I haven't attached the "coupling hook" that was originally there, as I may fit a kadee myself later|
I also fabricated a replacement cabside step from brass sheet, using the other one as a pattern. My replacement does not have the bolt detail of the original lost wax casting, but that was a detail I could live without.
|Shows the missing cabside step|
|My replacement step. I used two different solders for this. The steps were attached with high temp 60/40 resin core, but the step was attached to the body with low temp 144 degrees.|
Preparations for painting include stripping back the gold paint, and pickling in vinegar prior to painting with self-etch black.
|After paint stripping, the tarnish of the tender really was evident, more than the loco itself. The models are in the small container that I used for the vinegar picking solution|
|Not the best picture, but you get the idea. The tender has not yet been reassembled - it just looked better with the parts roughly placed in the right spot|
Monday’s winter weather here was quite nice, and I did get the main painting done in the relative warmth of the afternoon sun.
Dockyard VR R class.
What am I doing with a Victorian steam engine? Why indeed? Well, I spied this model at a Trains Planes and Automobile auction a year ago, listed as a “japanese brass loco”. Well, I knew what it was from the shape, but one always has to factor in some leeway. For instance, I only got a single picture, TPA offer no guarantees, and I was not able to physically attend the auction in person. So I placed a modest bid, and was successful.
|The TPA auction catalogue picture of the R class. note the clever way the tender is hiding the running gear|
A week later, the loco was delivered to me in a mess. It had been victim of the foam monster (the one picture on the TPA website showed the tender in front of the loco running gear, so the extent of the foam issue was hidden). More disturbingly, it had been posted without adequate packing inside the box. The damage was extensive. The worst was that the tender had acted as a hammer, and noticeably depressed the smoke box cover on top of the boiler.
|How not to post a loco. If it was an ebay purchase, I could have demanded compensation, or sent the model back. It wasn't an option with TPA|
|Note the depression on top of the smokebox.|
|More evidence of the foam damage|
|The loco body in the homemade cradle|
|The chassis was also heavily foam affected|
|After cleanup with no more than a toothbrush, the chassis was looking much better|
Fixing the depression was an exercise in luck. I first needed to create a hole at the bottom of the boiler (out of sight from normal viewing, so I could punch the brass back into shape. I modified the head of a large nail to act as a panel beating tool, and slowly tapped away onto a block of wood.
|New hole made in the boiler, and the modified nail I used as the panel beating punch|
Whilst not perfect, after adding some filling solder, filing, and wet-n-dry, I hope it will be difficult to tell the repair after painting. And yes, it will have to be R766 – the R class being standard gauged.
I hope that you all were able to spend some quality time working on your models.
Until next time